How not to run AutoTrain

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Joined
May 25, 2006
Messages
1,563
Location
Central Florida
After visiting family and friends in the northeast, we decided to take AutoTrain home on Sunday May15. Big mistake. Sunday morning I looked at the inbound train to Lorton knowing that it would turn that afternoon for our train that was due to leave at 5pm. It was running about 8 hours late as a result of successive days of late operation resulting from various mishaps. So, how could our train leave on time at 5pm as the Amtrak app still showed? Later I called customer relations and they confirmed what I suspected. Our train wouldn’t leave until ‘later’ but we should check in no later than 6:30pm and they advised having dinner before we arrived at the station. I knew this was going to be one of ‘those’ trips. One of the mechanical guys working on the inbound train told me the train would be annulled on Tuesday to catch up.

I’ll get into some of the details in a moment but for those of us with ADD I’ll summarize. We boarded the train at midnight, left Lorton at 1:30am and arrived Sanford at 8:15pm on Monday – about 10 hours late. In between we dined on snacks and fast food and tried to groggily recovery from the night before. So, the trip was a disaster but being optimistic there were some positive things about it. Our sleeper was mechanically good, if a bit tired cosmetically, the crew was excellent, CSX did a decent job of dispatching, and there is hope for the future. With that I’ll comment on a few things.

Lorton station was a roomy and pleasant place to hang out for 6 hours. My wife knitted and chatted with other passengers including those from the late inbound train who were waiting for their cars to be unloaded. I strolled the platforms and watched the inbound and outbound trains being unloaded and reloaded as well as a great view of the old RF&P and the many trains on it. My wife said an inbound passenger who was a regular snowbird on AutoTrain was exhausted. They had a full load waiting for the train and then the AC went out on a hot afternoon in Sanford. Passengers were livid and many gave up and drove. She tried to book on the next day’s AT but was told it was sold out and would be until June 10. To Amtrak’s credit when we arrived at Lorton they handed out snack boxes and water then a little later, maybe 8pm, gave out Subway subs.

Unlike other stations, the boarding location for each car was shown on the platform and it was easy to board once the train opened up at midnight. It had arrived at 8:30 and a group of cleaners was ready to go to work while mechanical people were servicing it, including a honey bucket truck! Unlike Sanford all the passenger cars could fit on the one platform. When it arrived the auto carriers were cutoff in the yard for the switch engine to spot at the six unloading racks (5 railcars on each with one track respotted). The servicing guys worked from the other side of the train so passengers were free to wander throughout the platform and surrounding station area. No gate ****’s!

Our train had 4 coaches, the coach café/lounge, 5 sleepers, the diner, sleeper lounge, and three more sleepers. The two all bedroom sleepers, including ours, were on either side of the diner and lounge. Our attendant was attentive and helpful and the rest of the crew we saw seemed to be too. It had to be tough on them too. As we arrived Sanford there was an announcement intended for the crew that said ‘crew number 3, be back on board a midnight’ for the return trip.

Even though AutoTrain is considered a premier train, the staffing bug has bit it too. There was one person in the diner, which was not open to passenger. He and a couple trainees prepared and handed out our meal boxes. Most ate in their rooms or a few in the unstaffed sleeper lounge next to the diner. We got the continental breakfast which was ok and included a hot breakfast sandwich, OJ, cereal, milk, coffee cake and banana. A coffee urn was set up in the lounge, there was none in the sleeper although there was ice.. Lunch was what I’ll call Dinty Moore pilaf. It was ok especially after I poured some of our glass of red wine into it. We were served this about 2pm and then around 6 we stopped in Jax so they could load on pizzas for everyone. So much for fine fining on Amtrak.

As I mentioned CSX did ok with the train given it’s late operation that wasn’t even close to its time slot. We left Lorton about 8 ½ hours late and arrived Sanford about 10 hours late. We passed many freights sitting in sidings. In the late morning an announcement was made that because the temperature that afternoon would be above 90, a heat related speed restriction had been issued. In addition we made the unscheduled pizza stop in Jax and went slowly through a long stretch around Palatka where there was track work. Fortunately the our train had a relatively light load so our car was unloaded quickly and we were home an hour after arrival in Sanford.

So why do I feel optimistic about the future? One of the OBS staff said they were hiring employees as fast as they could and fully intended to go back to full service dining as well as staff the sleeper lounge. We have kept contact with an SCA from a prior trip and he said they have hired 6 for AutoTrain and hiring 6 more. The changes can’t come soon enough as we (and a lot of fellow passengers) won’t ride it again until it returns to its former service level. The morning after our arrival I received a call from Amtrak guest relations. They apologized for the poor service and offered a full credit for the value of our tickets. They also gave me the email to send comments to their management, which I will do (although I think it’s just a generic email address: [email protected]). But at least they were a bit proactive and let’s hope they follow through as we’d like to take it in October. I’ll post a few photos later.
 
Actually, I think Amtrak did the best they could do. The Auto train does not serve lunch. And the weird operating hours because of delays must have messed up the stocking process. The fact of the matter is that Amtrak operated the train and did its best to feed the passengers. I am not sure what caused the initial cascade of delays, but if it was not Amtrak related then Amtrak did its best.

Canceling a train and then not accommodating the passengers is absolutely the worst thing. Yes, they could just drive, but still it is not a great solution.
 
I guess I waited too long to edit my report so I'll add photos as a separate message. Steve, I'm sure Amtrak did the best they could but for most passengers that was of little comfort. This is the first batch of photos.

Since Amtrak had suggested we have dinner before going to the station we found a delightful restaurant, the Harbour Grille, about 10 minutes away at the I-95 Woodbridge exit. Great place to spend the afternoon and even had a partial view of the SuperStar behind the US 1 bridge.

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When we arrived at the station snack boxes were handed out. Later we dined on subs.


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To pass the time I wandered outside and saw many trains from our great vantage point. This was a regional heading south.

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Amtrak was doing extensive tie replacement in the yard. The repair shop is in the distance. the switch engine was ready to go to work in a couple hours.

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The station had nice grounds including a small park and a kids play area that was well used.

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When we arrived they had starting staging the vehicles for loading. I asked why we had to be there at 6:30 when the train wouldn't board until midnight. They said if they hadn't we would leave two hours later as they could start reloading as soon as the inbound was unloaded.

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The six tracks for handling vehicles were ready for the inbound. When we arrived they had us put down on our windows I guess to make it easier for the drivers to load the cars. Notice the dark clouds in the backround.

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And of course a sudden storm blew in with a mad scramble to raise the windows. It was a driving rain that turned into a gentle one most of the evening. The switch engine headed out to the end of the yard ready to grab the auto carriers when the train arrived and the cars were cut off before the rest of the train arrived on the platform.

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With the storm arriving so did the inbound train making the unloading job even harder . A tractor was on one of the auto carrier and hauled off a wagon full of motorcycles. Two wagons were waiting to be relaoded.

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Meanwhile the passngers for our train waited patiently for the boarding that began at midnight. With the good signage it was easy to find our car.

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We awoke the next morning to have hot coffee and our breakfast ready for us. It wasn't the dining car experience but still feeling groggy it was nice to curl up in our room and enjoy it.

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It was a long day but it was nice to see parts of the railroad that would normally be in darkness. We left Florence around 9am spent a pleasant day with our menu surprises arriving about 1pm for the dinty moore type meal and the pizza around 6. No, that's not apple juice in the glasses, we needed it. We were disappointed that the dining car was not open to passngers but we were promised it would be as soon as proper staffing levels return.

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The lounge car was well used during the day although some repairs were needed and fast food type carry out created mountains of trash.

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We liked the all bedroom car as it seemed quieter, but the interior was dated with that carpeting on the walls.

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At last we arrived at 8:15pm and AutoTrain had one last day of late operation before being annulled. We'll take it again - when full service is restored. The outbound train was scheduled to board at midnight - again.
 
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