The Richmond newspaper reported that 195 broke down outside of Alexandria yesterday.
http://www2.timesdispatch.com/rtd/news/loc...-224801/324239/ It seems that the passengers were stranded for some time and according to the Amtrak site, the train arrived RVR 9 hours and 7 minutes late. I am rather surprised that since the train was not that far from WAS, it took that long to get another engine.
Well, as a passenger on 99, the train that ended up being tasked to rescue 195, I can say that all was not entirely well with us either.
We left Washington Union Station (WAS) only about 5 minutes late (5:05), only to be stopped just after CP Virginia, to wait on stacked up freight traffic across the Potomac to move North. After holding for a half hour or so, we were given clearrance to proceed across the long bridge into Virginia, where I noticed at least 3 more CSX freights waiting to head north.
We continued southbound, at a fairly slow pace, stopped at Alexandria, and proceeded South.We eventually stopped, waiting for a "disabled freight train" to be cleared out of the way. It turns out that this is actually 195.
Eventually we make a backing move North, while changing tracks from 2 to 4 to position us for evental connection to 195. (I assume that this was the Auto Train lead at Lorton, although it was difficult to tell at the time due to a lack of illumination.
We then proceeded to WAIT for about 3 hours, due to a "signal failure" preventing our further movement.
Once CSX finally got the signals working, we reversed back South, crossing back to track 3, and proceeded to wait for 195. It seems that the original plan was to have 195 approach us and connect, but this proved to not be possible.
We then reversed until we were almost to Lorton, where we finally made the coupling to the stranded 195.
After another half hour for connecting trainlines etc, etc, we again proceeded Southbound, where we proceeded to make TWO stops at each of the scheduled locations, one for passengers on 99, and a second for passengers on 195. This included a single stop at Woodbridge, which is
NOT normally one of 99's stops! This was one enormously long train at this point.
We finally pulled into Richmond (RVR) at about 2:15
. The amalgamation train completely filled the platform at Richmond!
While I was pleased that we were able to help out, many of the other passengers on 99 were not so happy about the delays. The crew on 99 was pretty good at keeping us pax informed, but most of the information appeared to be perceived as inaccurate or BS <_<
My regrets were: that I did not have a scanner to listen in on the actual discussions, that there was not enough light to get a credible photo of the enormous train stopped at Richmond :angry: , and that my wife, waiting at home, was worried and annoyed.
All in all an exciting night. That is what I get for chancing the first day of full operations on the RF&P after over a week of annulled trains!!!